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An operator
had been unsuccessful in previous attempts to fish an anchor and 300'
of tubing from a depth of 7500', in an old well in Garvin County, Oklahoma,
because of several deep casing leaks that had been acting as thief zones,
preventing the circulation of fill-up out of the hole, A review of the
casing inspection log led to the decision to spot two 25 bbl slugs of
Leakblock-HD polymer over severe leaks noted at 5800' and 4200', respectively.
The polymer
gels were spotted and bull head squeezed into the leaks, then allowed
to set 2 hours. Although the operator previously had no returns to surface
while attempting to wash-over the tubing, after the polymer squeeze, the
well was reverse circulated with nearly full returns at the surface. The
operator went on to fish the tubing & anchor out of the hole with no further
problems. The well was re-completed and has been returned to production.

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